BP Assumes “A Little Blame” for the Deepwater Horizon Oil Spill in a New Report
Below is the press release that was issued by BP regarding their internal investigation of the Deepwater Horizon Oil Spill tragedy. They are willing to admit to “some” blame but the report concludes that several companies and work teams were at fault. This is reminiscent of the congressional hearing where the CEOs of Haliburton, BP and Transocean kept pointing fingers at each other rather than admit liability.
A report released by BP today concludes that decisions made by “multiple companies and work teams” contributed to the accident which it says arose from “a complex and interlinked series of mechanical failures, human judgments, engineering design, operational implementation and team interfaces.”
- The cement and shoe track barriers – and in particular the cement slurry that was used – at the bottom of the Macondo well failed to contain hydrocarbons within the reservoir, as they were designed to do, and allowed gas and liquids to flow up the production casing;
- The results of the negative pressure test were incorrectly accepted by BP and Transocean, although well integrity had not been established;
- Over a 40-minute period, the Transocean rig crew failed to recognise and act on the influx of hydrocarbons into the well until the hydrocarbons were in the riser and rapidly flowing to the surface;
- After the well-flow reached the rig it was routed to a mud-gas separator, causing gas to be vented directly on to the rig rather than being diverted overboard;
- The flow of gas into the engine rooms through the ventilation system created a potential for ignition which the rig’s fire and gas system did not prevent;
- Even after explosion and fire had disabled its crew-operated controls, the rig’s blow-out preventer on the sea-bed should have activated automatically to seal the well. But it failed to operate, probably because critical components were not working.
“To put it simply, there was a bad cement job and a failure of the shoe track barrier at the bottom of the well, which let hydrocarbons from the reservoir into the production casing. The negative pressure test was accepted when it should not have been, there were failures in well control procedures and in the blow-out preventer; and the rig’s fire and gas system did not prevent ignition.
“Based on the report, it would appear unlikely that the well design contributed to the incident, as the investigation found that the hydrocarbons flowed up the production casing through the bottom of the well,” Hayward said.
“This was a tragic accident that resulted in the loss of 11 lives and impacted the communities and the environment along the Gulf Coast region. We deeply regret this event. We have sought throughout to step up to our responsibilities. We are determined to learn the lessons for the future and we will be undertaking a broad-scale review to further improve the safety of our operations. We will invest whatever it takes to achieve that. It will be incumbent on everyone at BP to embrace and implement the changes necessary to ensure that a tragedy like this can never happen again.”
Chairman of the Board Carl-Henric Svanberg commented: “I believe this report will be of significant value in helping the overall understanding of how this tragedy occurred. It is of the utmost importance to the Board to ensure that BP learns from this and further enhances the safety of its operations for the future.”
The company said it expected a number of the investigation report’s findings to be considered relevant to the oil industry more generally and for some of the recommendations to be widely adopted.
BP said the report was based on information available to the investigating team. It noted that additional relevant information may be forthcoming, for example, when Halliburton’s samples of the cement used in the well are released for testing and when the rig’s blow-out preventer is fully examined now that it has been recovered from the sea-bed. There will also be additional information from the multiple ongoing US government investigations.
The investigation report is available online, together with an accompanying video.
Short URL: http://www.oceanpowermagazine.net/?p=2168





